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The engine
which suffered damage was an eight-cylinder two-stroke
marine diesel engine arranged to drive a large
alternator. The first indications that it had a problem
were loud knocking sounds. Unfortunately, before the
engine could be brought to a stop, one of its connecting
rods separated from the crank pin and emerged from the
crankcase, causing substantial damage. The final state
of the connecting rod can be judged from the picture
opposite. As the various damaged parts became
accessible, possible alternative causes were tested for
credibility. By this process, attention was increasingly
drawn to the need to find the crank bearing bolts, which
were not initially accessible. When they were retrieved,
one of them was found to be virtually intact, but
without its nut. This nut, its locking device and
locking screw were all found separately. The nut threads
for about one and a half turns nearest to the lower face
were seen to have been damaged by axial shear.
About one quarter of the first turn, although
present, had been separated from the nut around its
circumference. The other bolt had broken under severe
combined tensile and bending load and its nut, with
locking device and screw, was still present on the
broken end. Furthermore, a bolt in a different
connecting rod was found to be 1 mm slack, with its nut
locking device and locking screws correctly fitted.
This evidence
clearly showed that the slackening and loss of the
intact bolt was the initiating cause of the engine
damage. In searching for the reason why the bolt became
slack, the effects on the bolt of possible cylinder
malfunctions were calculated and physical tests of
similar bolts were conducted. The key finding from this
work was that if the bolt had been properly tightened,
the probability that sufficient torque could have been
generated to loosen the nut against the frictional
resistance of the threads and of the nut face was
minimal. The torque due to tensile load, which normally
acts to unscrew a nut, was found to be one eighth of the
frictional torque resisting such movement. It was
concluded, therefore, that the damage resulted because
the bolt had not been properly tightened to the correct
tensile load.
The routine
maintenance procedures adopted for this installation
involved periodic checks of the bolt tension. The method
used was to slacken and re-tension the bolts and, as
such, this procedure had the potential to introduce
error. |